More jetting problems....
Damn carb came with a #91 main and #32 pilot, BBK came with a #90 main. Ran fine but wouldn't idle right. Switched the pilot to a #30, everything went great for a few weeks til my head gasket went. Switched the head gasket out for a new one, ran like shit and would barely idle.... Too rich. Stayed with the 30 pilot, swapped to a 88 main, ran best when the mixture screw was at it's leanest. Threw in an 85 main, wouldn't start at the most lean setting, turned the mixture screw to almost the richest setting, started and died.
Haven't fucked with it since thwn, I'll figure it out tomorrow :lol: