built turbo ls, what happened?

Prozon

Kris
Like I said, i've seen stock sleeves handle up to 600hp.. makes me think he bored the block out too much and weakened the sleeves a lot.
 

mcplayer21

New Member
it was bored out over .20 but i think what made it crack was the dam block guard that i put on..crack starts there and makes its way down
 

DaddyBuiltRacing

Resident Asshole
Block gaurds are known to warp the walls not crack them. My guess is you went lean and caused detonation, thus causing the sleeve to say goodbye
 

mcplayer21

New Member
dam this is my second turbo motor in my integra first was stock internals and piston disinegrated while rod bent and smashed the wall so i this motor and built it and now 2 weeks later this happened..what should i do should i sleeve the next motor i get? haven't had time to enjoy car lol
 


DaddyBuiltRacing

Resident Asshole
Sounds to me like you've had a shitty tune both times. Pistons don't just desenegrate themselves and sleeves don't crack without detonation
 

mcplayer21

New Member
yea the parts are fine they all are reusable and im guessing it was the tune aswell because both builds together didnt even last a month..but i decided to just send my other block to laskey racing heard nothing but good news from them and already spoke with them and there customer service was great
 


mcplayer21

New Member
haha good to hear starting reading your build and wow what good quality build your doing good luck on it deff seeing 10s in that
 

DaddyBuiltRacing

Resident Asshole
Thanks man, should see low 12s if not high 11's next time at the track on 10psi, might raise it a little more just to be sure haha. Would've went higher yesterday but lap top started running out of battery plus we was hungry haha. I did rape a turbo LS last night that was on 10psi as well. Trying to get the vids uploaded from buddies facebook onto my youtube account. Leave some comments on my build thread, always like reading them
 
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